



I'm on my 3rd head gasket, refitting the head is getting silly now, so lets throw this one on the forum.




I have rebuilt the top end after blowing head gasket, now the HG seems to just fail.


Crusing at 3k warming motor through cased it to fail using a genuine REV3 MLS head gasket.





Originally the cometic 1.6mm went when I was racing, it still ran, with a chance of over heating, then a 1.5mm MLS





I drag raced on the cometic for a year or two so overall the unit works, I've broken something.




The block looks ok

I have used



I have ARP head bolts and have been torquing up to 65ft lb in three stages with moly lube, in correct sequence.


I'm stumped.




Could it be the ARP head studs?

Oh it's a REV1/2 head.
